乱人伦人妻中文字幕在线,亚洲精品人成无码中文毛片,亚洲精品久久久久久久观小说,五月丁香综合激情六月久久



A brief analysis of the transformation process of coating production line
Time:2012-10-22 11:51:38

       The painting production line of the complete machine is designed by the former First Design and Research Institute of machinery Industry, which adopts the advanced and mature industrial art in China at that time, and improves the mechanization and automation level of the painting production line, so as to improve the working environment and reduce the labor intensity of workers. At the same time, it has earnestly implemented the relevant state laws and regulations, norms and standards, and worked hard to do a good job in environmental protection and occupational safety and health.


       The whole production line by line, drying, screening, drying, paint on the surface and, offline 7 station such as composition, except on and off the five stations by an organic water drying room, shielding room, water spray paint room, flow flat room and dry room of a closed production line, and workshop is separated, ensures the whole paint areas relatively clean. In addition, a complete machine cleaning section is built at one end of the workshop for secondary cleaning of the complete machine. The whole machine adopts double board ground chain transportation to improve the mechanization level.


       Process flow: water gun oil removal cleaning -- on line -- hot air drying -- shielding -- surface paint spraying -- leveling -- drying -- removing shielding -- off line.


       The operation time of each station is 45min, and the cycle time of the pipeline can be adjusted appropriately according to the actual use.


       The paint varieties are komatsu yellow acrylic polyurethane enamel and the spray gun is electrostatic mixed air spray gun.


       The coating production line can produce 2000 loaders per year when only units are arranged for production. The total number of designers in the coating workshop is 24, including 16 production workers. The average annual output of each production worker is 142 loaders.


Second, the question raises

       After 2003, due to the country to increase the investment in infrastructure, the loader industry into the good situation of flourishing production and marketing, several major loader production enterprises have reached their maximum output record. At the same time, each manufacturer has improved the appearance quality. The paint is mainly used to color the loader. The loader's appearance color is divided into two parts, which changes the loader's single color for a long time.


       With the increase of loader output and the extensive use of exterior paint color registration, several problems occurred in the application process of complete machine coating line:

       (1) the surface spray paint tinted homework makes loader shorter time () down on a painting area, and screen instead of to shorten the time, and extension of trend, make the whole assembly line beat changed, when in low yield, but increased the waiting time for some station, yield increase and then need to be partially blocked work offline.

       (2) Due to the shortened beat of the entire production line, there is a heating process in the water mark drying room, so that the temperature just rises to the specified temperature and sometimes even does not rise to the specified temperature, it needs to be transferred to the next station, which cannot play a role at all. However, the water mark drying room is a pass-through type, and the temperature immediately drops to the ambient temperature after the door is opened.

       (3) The drying room also has the same problem as the water mark drying room, which cannot give full play to the drying role.

       (4) The door of each chamber adopts pneumatic door, the time of switch is long, fully open or completely close is about 3-5min, in the whole beat is long (45min), do not feel, after the beat is shortened it seems a little too long.

       (5) the utilization rate of the waste gas treatment device is too low, because the exhaust gas in the paint room is fully mixed with water, and the air volume is large, so the organic solvent content discharged into the atmosphere can meet the emission standards. The drying chamber USES the hot air circulation, a small part of the exhaust gas emissions, this small part of the exhaust gas may exceed the standard, so most of the production lines have added activated carbon adsorption device.


3. Suggestions for improvement

       It is impossible to solve the above problems by using the current intermittent pass-through production line. To completely solve the above problem, only fundamentally change the production line type, or like a car factory adopted by type production line, continuous operation, every room body is longer, the whole production line without door, drying room a preliminary drying and strong cold area, and use the wind curtain interception heat, or use the Chambers and decorate, a spray room with 2-3 drying room, loader into the drying chamber immediately after spray paint, flat, drying in the process of heating up, some large-scale passenger car manufacturer both in this way.


Iv. Practical operation

With the increasing production of loaders, the measures taken by our company are as follows:

       1) After cleaning and removing oil, the loader should take the way of natural cooling and drying, pay attention to maintain balanced production, if the weather is bad, use the night time to dry.

       (2) When the production line is in operation, the water-mark drying room does not work, and most of the shielding work is carried out offline.

       (3) All the doors of the room are closed when painting, in order to save time. In this way, it is easy to cause the paint mist to fly to the shielding room and leveling room next to the paint room.

       (4) A new 720m2 hangar will be built for parking the loader sprayed with paint, and the painting and decoration work will be carried out here; When the temperature is low, use the evening time to dry.

       (5) Make some baffles of shield glass with tin sheet to save the time of shield glass.

    

       Through the above measures, the company has ensured the painting workshop in the case of no night shift, Nissan 15-20 loaders. Of course, the above measures are a little harmful to the production line. In order to improve the problem of drying in winter, the company plans to build a new drying room for drying the paint of the whole machine, and prepare to move the water-mark drying room below the line to play its role.

Service hotline

020-36860788

WeChat

Feedback

Feedback

主站蜘蛛池模板: 国产成人国拍亚洲精品| 精品国产乱码久久久久久郑州公司| 国产成人一区二区精品视频| 午夜内射中出视频| 国产精品无码综合区| 99国产精品久久久久久久久久久| 国产精品乱码久久久久久软件| 久久免费99精品国产自在现线| 无码国产精品一区二区免费3p | 国产精品久久久久久久伊一| 欧美交换配乱吟粗大免费看| 欧美日韩在线视频一区| 国产超碰av人人做人人爽| 少妇激情一区二区三区视频小说| 日韩吃奶摸下aa片免费观看| 亚洲精品国产美女久久久| 国产精品夜夜春夜夜爽久久小| 怡红院一区二区三区在线| 天天综合网在线观看视频| 国产蜜臀av在线一区尤物 | 男女做爰猛烈啪啪吃奶图片| 欧美成人在线视频| 亚洲另类激情综合偷自拍图片| 中国亚洲女人69内射少妇| 日本免费高清线视频免费| 国产精品成人无码久久久久久| 18禁女裸乳扒开免费视频| 无码国产成人午夜电影观看| 野花香社区在线视频观看播放 | 亚洲人成黄网站69影院| 国产亚洲精品久久久久蜜臀| 亚洲精品一区国产精品| 2020久热爱精品视频在线观看| 久久天天拍天天爱天天躁| 2020最新无码福利视频| 国产精品制服一区二区| 波多野成人无码精品电影| 999久久免费精品国产| 欧美亚洲另类 丝袜综合网| 国产sm鞭打折磨调教视频| 国产在沙发上午睡被强|